Have you experimented with any different size hardened ball bearings, or have you only done this with the 3/4" diameter size? Could you envision any benefit to going with a larger or smaller diameter ball bearing?
I own and have used the RW Hart tool that was designed and sold to do the same thing. The face of the punch that was used to compress the brass surrounding the primer pocket was too soft to endure long use. It worked well for several casings, but then it deformed more so than the brass case head. This was a tough one to figure. It shouldn't have required too much effort or expense to fabricate the punch out of steel that would be strong enough to deform/compress the brass, rather than vice versa.
I've not used your technique yet, but I view it as the better method. lightbulb I'll probably brainstorm a differing means to secure the ball bearing than using my bench vise. Perhaps a beefy piece of steel with a 5/8" diameter hole which supports the lower half of the ball bearing. Then set both on an anvil or a concrete floor and hammer away.
Finally got around to tightening up some primer pockets with this method today. Works much better than the RW Hart Tool.
I used a 5/8" ball bearing. Purchases a 10-pack months ago. I drilled a shallow indentation using a 1/2" drill bit into the surface of a 1/2" thick piece of plate steel that's only about 3"x3" square. This indentation served as a pocket to hold the ball bearing somewhat captive. Then I placed the 1/2" thick 3"x3" plate steel on top of the anvil type surface on my bench vice. That's where I hammered the primer pockets tight.
Use the biggest bolt that will fit through the case mouth. I ended up grinding down oversized grade 8 bolts on a bench grinder until they just cleared my case mouths. I tightened up primer pockets on 30/375 S.I. brass (parent cases 375 Ruger brass), on 280 RCBS Improved brass (parent cases 30-06 Lapua brass), on 338 Edge brass (parent cases RWS 404 Jeffery brass), and on some 25 RUM brass (parent cases 7mm RUM R-P brass).
Here's a tip. The bolt head that contacts the base of the interior of the cases has to be larger than the primer pocket hole. Otherwise you'll simply pop out the thin base in the bottom of the primer pocket where the flash hole is located. I used a factory bolt small enough to fit inside one of my 280 RCBS Improved cases and that's what happened. That's when I ground down a 5/16" Grade 8 bolt to barely clear the .284 case mouth. Then the end of the bolt was large enough to catch the meaty part of the case head and all was good.
On the two 25 RUM casings, I expanded the case mouth up to .284 using a K&M outside neck turning mandrel. Then I was able to use the same bolt that I'd used for the 280 RCBS Improved cases. Then I necked back down to .257 case neck by running the casings into a Redding 25 RUM full length sizer die, the same way I necked down the 7mm RUM brass in the first place. Kind of a pain in the ***.
I don't think this method will work well for smaller calibers cartridges, because the bolt will have to be small enough to clear the interior case neck and when the end of the bolt gets smaller than the primer pocket, or even just a little bigger than the primer pocket hole/diameter, then the bolt will rupture and ruin the thin base of the primer pocket where the flash hole is drilled/punched through.
I tightened up a few of the primer pockets tighter than desired. Then I simply used a K&M primer pocket uniforming tool in a battery powered drill to open the primer pocket back up a wee bit. This is probably an even better approach, because a greater depth of the primer pocket sidewall gets swaged down, and should therefore endure more shots than if a lesser depth of the primer pocket sidewall has been swaged down.